Attendance:
*Jessica
Agenda:
*Work on robot
Member comments/input:
*Saturday:
I attached the arm to the robot. The screws were on wrong on the servo bracket. They were to short, so we needed to replace them with longer screws. They held the servo bracket to the arm.
From testing the robot out, we need to drive the robot up the ramp backwards so that the motors propel the robot forward. We were going to attach the gears and motor to the arm so it can move. We couldn't figure out how to attach the tube so we switched to an axle. Then we had some problems with the size of the gear. We used the larger ones. But even after we set it all up, it STILL wouldn't move.
Sunday:Once we had the arm working we had some problems with it. It would slam down. We experimented a couple times and it finally vanished. But we couldn't get up the ramp because there was too much weight. I put the battery in the front/back and it WORKED!!!
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